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commit 64b12a68a9f74bb32d8efd7af1ad8a2ba02fc884
"mmc: core: fix prepared requests while doing bkops"
is fixing a bug in the wrong way. A bug in the MMCI
device driver is fixed by amending the MMC core.
Thinking about it: what the pre- and post-callbacks
are doing is to essentially map and unmap SG lists
for DMA transfers. Why would we not be able to do that
just because a BKOPS command is sent inbetween?
Having to unprepare/prepare the next asynchronous
request for DMA seems wrong.
Looking the backtrace in that commit we can see what
the real problem actually is:
mmci_data_irq() is calling mmci_dma_unmap() twice
which is goung to call arm_dma_unmap_sg() twice
and v7_dma_inv_range() twice for the same sglist
and that will crash.
This happens because a request is prepared, then
a BKOPS is sent. The IRQ completing the BKOPS command
goes through mmci_data_irq() and thinks that a DMA
operation has just been completed because
dma_inprogress() reports true. It then proceeds to
unmap the sglist.
But that was wrong! dma_inprogress() should NOT be
true because no DMA was actually in progress! We had
just prepared the sglist, and the DMA channel
dma_current has been configured, but NOT started!
Because of this, the sglist is already unmapped when
we get our actual data completion IRQ, and we are
unmapping the sglist once more, and we get this crash.
Therefore, we need to revert this solution pushing
the problem to the core and causing problems, and
instead augment the implementation such that
dma_inprogress() only reports true if some DMA has
actually been started.
After this we can keep the request prepared during the
BKOPS and we need not unprepare/reprepare it.
Fixes: 64b12a68a9f7 ("mmc: core: fix prepared requests while doing bkops")
Cc: Srinivas Kandagatla <srinivas.kandagatla@linaro.org>
Signed-off-by: Linus Walleij <linus.walleij@linaro.org>
Tested-by: Srinivas Kandagatla <srinivas.kandagatla@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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This fixes a race condition that may occur whenever ST micro busy end
interrupt is raised just after being unmasked but before leaving mmci
interrupt context.
A dead-lock has been found if connecting mmci ST Micro variant whose amba
id is 0x10480180 to some new eMMC that supports internal caches. Whenever
mmci driver enables cache control by programming eMMC's EXT_CSD register,
block driver may request to flush the eMMC internal caches causing mmci
driver to send a MMC_SWITCH command to the card with FLUSH_CACHE operation.
And because busy end interrupt may be mistakenly cleared while not yet
processed, this mmc request may never complete. As a result, mmcqd task
may be stuck forever.
Here is an instance caught by lockup detector which shows that mmcqd task
was hung while waiting for mmc_flush_cache command to complete:
..
[ 240.251595] INFO: task mmcqd/1:52 blocked for more than 120 seconds.
[ 240.257973] Not tainted 4.1.13-00510-g9d91424 #2
[ 240.263109] "echo 0 > /proc/sys/kernel/hung_task_timeout_secs" disables this message.
[ 240.270955] mmcqd/1 D c047504c 0 52 2 0x00000000
[ 240.277359] [<c047504c>] (__schedule) from [<c04754a0>] (schedule+0x40/0x98)
[ 240.284418] [<c04754a0>] (schedule) from [<c0477d40>] (schedule_timeout+0x148/0x188)
[ 240.292191] [<c0477d40>] (schedule_timeout) from [<c0476040>] (wait_for_common+0xa4/0x170)
[ 240.300491] [<c0476040>] (wait_for_common) from [<c02efc1c>] (mmc_wait_for_req_done+0x4c/0x13c)
[ 240.309224] [<c02efc1c>] (mmc_wait_for_req_done) from [<c02efd90>] (mmc_wait_for_cmd+0x64/0x84)
[ 240.317953] [<c02efd90>] (mmc_wait_for_cmd) from [<c02f5b14>] (__mmc_switch+0xa4/0x2a8)
[ 240.325964] [<c02f5b14>] (__mmc_switch) from [<c02f5d40>] (mmc_switch+0x28/0x30)
[ 240.333389] [<c02f5d40>] (mmc_switch) from [<c02f0984>] (mmc_flush_cache+0x54/0x80)
[ 240.341073] [<c02f0984>] (mmc_flush_cache) from [<c02ff0c4>] (mmc_blk_issue_rq+0x114/0x4e8)
[ 240.349459] [<c02ff0c4>] (mmc_blk_issue_rq) from [<c03008d4>] (mmc_queue_thread+0xc0/0x180)
[ 240.357844] [<c03008d4>] (mmc_queue_thread) from [<c003cf90>] (kthread+0xdc/0xf4)
[ 240.365339] [<c003cf90>] (kthread) from [<c0010068>] (ret_from_fork+0x14/0x2c)
..
..
[ 240.664311] INFO: task partprobe:564 blocked for more than 120 seconds.
[ 240.670943] Not tainted 4.1.13-00510-g9d91424 #2
[ 240.676078] "echo 0 > /proc/sys/kernel/hung_task_timeout_secs" disables this message.
[ 240.683922] partprobe D c047504c 0 564 486 0x00000000
[ 240.690318] [<c047504c>] (__schedule) from [<c04754a0>] (schedule+0x40/0x98)
[ 240.697396] [<c04754a0>] (schedule) from [<c0477d40>] (schedule_timeout+0x148/0x188)
[ 240.705149] [<c0477d40>] (schedule_timeout) from [<c0476040>] (wait_for_common+0xa4/0x170)
[ 240.713446] [<c0476040>] (wait_for_common) from [<c01f3300>] (submit_bio_wait+0x58/0x64)
[ 240.721571] [<c01f3300>] (submit_bio_wait) from [<c01fbbd8>] (blkdev_issue_flush+0x60/0x88)
[ 240.729957] [<c01fbbd8>] (blkdev_issue_flush) from [<c010ff84>] (blkdev_fsync+0x34/0x44)
[ 240.738083] [<c010ff84>] (blkdev_fsync) from [<c0109594>] (do_fsync+0x3c/0x64)
[ 240.745319] [<c0109594>] (do_fsync) from [<c000ffc0>] (ret_fast_syscall+0x0/0x3c)
..
Here is the detailed sequence showing when this issue may happen:
1) At probe time, mmci device is initialized and card busy detection based
on DAT[0] monitoring is enabled.
2) Later during run time, since card reported to support internal caches, a
MMCI_SWITCH command is sent to eMMC device with FLUSH_CACHE operation. On
receiving this command, eMMC may enter busy state (for a relatively short
time in the case of the dead-lock).
3) Then mmci interrupt is raised and mmci_irq() is called:
MMCISTATUS register is read and is equal to 0x01000440. So the following
status bits are set:
- MCI_CMDRESPEND (= 6)
- MCI_DATABLOCKEND (= 10)
- MCI_ST_CARDBUSY (= 24)
Since MMCIMASK0 register is 0x3FF, status variable is set to 0x00000040 and
BIT MCI_CMDRESPEND is cleared by writing MMCICLEAR register.
Then mmci_cmd_irq() is called. Considering the following conditions:
- host->busy_status is 0,
- this is a "busy response",
- reading again MMCISTATUS register gives 0x1000400,
MMCIMASK0 is updated to unmask MCI_ST_BUSYEND bit.
Thus, MMCIMASK0 is set to 0x010003FF and host->busy_status is set to wait
for busy end completion.
Back again in status loop of mmci_irq(), we quickly go through
mmci_data_irq() as there are no data in that case. And we finally go
through following test at the end of while(status) loop:
/*
* Don't poll for busy completion in irq context.
*/
if (host->variant->busy_detect && host->busy_status)
status &= ~host->variant->busy_detect_flag;
Because status variable is not yet null (is equal to 0x40), we do not leave
interrupt context yet but we loop again into while(status) loop. So we run
across following steps:
a) MMCISTATUS register is read again and this time is equal to 0x01000400.
So that following bits are set:
- MCI_DATABLOCKEND (= 10)
- MCI_ST_CARDBUSY (= 24)
Since MMCIMASK0 register is equal to 0x010003FF:
b) status variable is set to 0x01000000.
c) MCI_ST_CARDBUSY bit is cleared by writing MMCICLEAR register.
Then, mmci_cmd_irq() is called one more time. Since host->busy_status is
set and that MCI_ST_CARDBUSY is set in status variable, we just return from
this function.
Back again in mmci_irq(), status variable is set to 0 and we finally leave
the while(status) loop. As a result we leave interrupt context, waiting for
busy end interrupt event.
Now, consider that busy end completion is raised IN BETWEEN steps 3.a) and
3.c). In such a case, we may mistakenly clear busy end interrupt at step
3.c) while it has not yet been processed. This will result in mmc command
to wait forever for a busy end completion that will never happen.
To fix the problem, this patch implements the following changes:
Considering that the mmci seems to be triggering the IRQ on both edges
while monitoring DAT0 for busy completion and that same status bit is used
to monitor start and end of busy detection, special care must be taken to
make sure that both start and end interrupts are always cleared one after
the other.
1) Clearing of card busy bit is moved in mmc_cmd_irq() function where
unmasking of busy end bit is effectively handled.
2) Just before unmasking busy end event, busy start event is cleared by
writing card busy bit in MMCICLEAR register.
3) Finally, once we are no more busy with a command, busy end event is
cleared writing again card busy bit in MMCICLEAR register.
This patch has been tested with the ST Accordo5 machine, not yet supported
upstream but relies on the mmci driver.
Signed-off-by: Sarang Mairal <sarang.mairal@garmin.com>
Signed-off-by: Jean-Nicolas Graux <jean-nicolas.graux@st.com>
Reviewed-by: Linus Walleij <linus.walleij@linaro.org>
Tested-by: Ulf Hansson <ulf.hansson@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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The void (*pre_req) callback in the struct mmc_host_ops vtable
is passing an argument "is_first_req" indicating whether this is
the first request or not.
None of the in-kernel users use this parameter: instead, since
they all just do variants of dma_map* they use the DMA cookie
to indicate whether a pre* callback has already been done for
a request when they decide how to handle it.
Delete the parameter from the callback and all users, as it is
just pointless cruft.
Signed-off-by: Linus Walleij <linus.walleij@linaro.org>
Acked-by: Jaehoon Chung <jh80.chung@samsung.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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The ST Micro-specific busy detection was made after the assumption
that only this variant supports busy detection. So when doing busy
detection, the host immediately tries to use some ST-specific
register bits.
Since the qualcomm variant also supports some busy detection
schemes, encapsulate the variant flags better in the variant struct
and prepare to add more variants by just providing some bitmasks
to the logic.
Put the entire busy detection logic within an if()-clause in the
mmci_cmd_irq() function so the code is only executed when busy
detection is enabled, and so that it is kept in (almost) one
place, and add comments describing what is going on so the
code can be understood.
Tested on the Ux500 by introducing some prints in the busy
detection path and noticing how the IRQ is enabled, used and
disabled successfully.
Cc: Srinivas Kandagatla <srinivas.kandagatla@linaro.org>
Signed-off-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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There was some confusion in the CPSM (Command Path State Machine)
and DPSM (Data Path State Machine) regarding the naming of the
registers, clarify the meaning of this acronym so the naming is
understandable, and consistently use BIT() to define these fields.
Consequently name the register bit defines MCI_[C|D]PSM_* and
adjust the driver as well.
Include new definitions for a few bits found in a patch from
Srinivas Kandagatla.
Cc: Srinivas Kandagatla <srinivas.kandagatla@linaro.org>
Signed-off-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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Commit 9250aea76bfc ("mmc: core: Enable runtime PM management of host
devices"), made some calls to the runtime PM API from the driver
redundant. Especially those which deals with runtime PM reference
counting, so let's remove them.
Cc: Russell King <linux@arm.linux.org.uk>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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The header file asm/sizes.h is unnecessary, let's remove it.
This also allows to compile under X86 arch.
Signed-off-by: Wang Hongcheng <annie.wang@amd.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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The Nomadik variant supports 8bit mode for (e)MMC cards.
Signed-off-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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commit 4956e10903fd ("ARM: 6244/1: mmci: add variant data and default
MCICLOCK support") added variant data for ARM, U300 and Ux500 variants.
The Nomadik NHK8815/8820 variant was erroneously labeled as a U300
variant, and when the proper Nomadik variant was later introduced in
commit 34fd421349ff ("ARM: 7378/1: mmci: add support for the Nomadik MMCI
variant") this was not fixes. Let's say this fixes the latter commit as
there was no proper Nomadik support until then.
Cc: stable@vger.kernel.org
Fixes: 34fd421349ff ("ARM: 7378/1: mmci: add support for the Nomadik...")
Signed-off-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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Signed-off-by: Bjorn Andersson <bjorn.andersson@sonymobile.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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DMA configuration has been removed from function mmci_dma_setup but the
local mask variable was not removed. This remains unused hence remove
it from the function and operations on it
Signed-off-by: Pramod Gurav <pramod.gurav@smartplayin.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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Previously the pm_runtime_put() caused the device to be runtime PM
suspended, but then immediately being resumed when we add the host.
Prevent this unnecessary runtime PM suspend/resume cycle during
->probe() by moving the call to pm_runtime_put() after mmc_add_host().
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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git://git.kernel.org/pub/scm/linux/kernel/git/rafael/linux-pm
Pull ACPI and power management updates from Rafael Wysocki:
"This time we have some more new material than we used to have during
the last couple of development cycles.
The most important part of it to me is the introduction of a unified
interface for accessing device properties provided by platform
firmware. It works with Device Trees and ACPI in a uniform way and
drivers using it need not worry about where the properties come from
as long as the platform firmware (either DT or ACPI) makes them
available. It covers both devices and "bare" device node objects
without struct device representation as that turns out to be necessary
in some cases. This has been in the works for quite a few months (and
development cycles) and has been approved by all of the relevant
maintainers.
On top of that, some drivers are switched over to the new interface
(at25, leds-gpio, gpio_keys_polled) and some additional changes are
made to the core GPIO subsystem to allow device drivers to manipulate
GPIOs in the "canonical" way on platforms that provide GPIO
information in their ACPI tables, but don't assign names to GPIO lines
(in which case the driver needs to do that on the basis of what it
knows about the device in question). That also has been approved by
the GPIO core maintainers and the rfkill driver is now going to use
it.
Second is support for hardware P-states in the intel_pstate driver.
It uses CPUID to detect whether or not the feature is supported by the
processor in which case it will be enabled by default. However, it
can be disabled entirely from the kernel command line if necessary.
Next is support for a platform firmware interface based on ACPI
operation regions used by the PMIC (Power Management Integrated
Circuit) chips on the Intel Baytrail-T and Baytrail-T-CR platforms.
That interface is used for manipulating power resources and for
thermal management: sensor temperature reporting, trip point setting
and so on.
Also the ACPI core is now going to support the _DEP configuration
information in a limited way. Basically, _DEP it supposed to reflect
off-the-hierarchy dependencies between devices which may be very
indirect, like when AML for one device accesses locations in an
operation region handled by another device's driver (usually, the
device depended on this way is a serial bus or GPIO controller). The
support added this time is sufficient to make the ACPI battery driver
work on Asus T100A, but it is general enough to be able to cover some
other use cases in the future.
Finally, we have a new cpufreq driver for the Loongson1B processor.
In addition to the above, there are fixes and cleanups all over the
place as usual and a traditional ACPICA update to a recent upstream
release.
As far as the fixes go, the ACPI LPSS (Low-power Subsystem) driver for
Intel platforms should be able to handle power management of the DMA
engine correctly, the cpufreq-dt driver should interact with the
thermal subsystem in a better way and the ACPI backlight driver should
handle some more corner cases, among other things.
On top of the ACPICA update there are fixes for race conditions in the
ACPICA's interrupt handling code which might lead to some random and
strange looking failures on some systems.
In the cleanups department the most visible part is the series of
commits targeted at getting rid of the CONFIG_PM_RUNTIME configuration
option. That was triggered by a discussion regarding the generic
power domains code during which we realized that trying to support
certain combinations of PM config options was painful and not really
worth it, because nobody would use them in production anyway. For
this reason, we decided to make CONFIG_PM_SLEEP select
CONFIG_PM_RUNTIME and that lead to the conclusion that the latter
became redundant and CONFIG_PM could be used instead of it. The
material here makes that replacement in a major part of the tree, but
there will be at least one more batch of that in the second part of
the merge window.
Specifics:
- Support for retrieving device properties information from ACPI _DSD
device configuration objects and a unified device properties
interface for device drivers (and subsystems) on top of that. As
stated above, this works with Device Trees and ACPI and allows
device drivers to be written in a platform firmware (DT or ACPI)
agnostic way. The at25, leds-gpio and gpio_keys_polled drivers are
now going to use this new interface and the GPIO subsystem is
additionally modified to allow device drivers to assign names to
GPIO resources returned by ACPI _CRS objects (in case _DSD is not
present or does not provide the expected data). The changes in
this set are mostly from Mika Westerberg, Rafael J Wysocki, Aaron
Lu, and Darren Hart with some fixes from others (Fabio Estevam,
Geert Uytterhoeven).
- Support for Hardware Managed Performance States (HWP) as described
in Volume 3, section 14.4, of the Intel SDM in the intel_pstate
driver. CPUID is used to detect whether or not the feature is
supported by the processor. If supported, it will be enabled
automatically unless the intel_pstate=no_hwp switch is present in
the kernel command line. From Dirk Brandewie.
- New Intel Broadwell-H ID for intel_pstate (Dirk Brandewie).
- Support for firmware interface based on ACPI operation regions used
by the PMIC chips on the Intel Baytrail-T and Baytrail-T-CR
platforms for power resource control and thermal management (Aaron
Lu).
- Limited support for retrieving off-the-hierarchy dependencies
between devices from ACPI _DEP device configuration objects and
deferred probing support for the ACPI battery driver based on the
_DEP information to make that driver work on Asus T100A (Lan
Tianyu).
- New cpufreq driver for the Loongson1B processor (Kelvin Cheung).
- ACPICA update to upstream revision 20141107 which only affects
tools (Bob Moore).
- Fixes for race conditions in the ACPICA's interrupt handling code
and in the ACPI code related to system suspend and resume (Lv Zheng
and Rafael J Wysocki).
- ACPI core fix for an RCU-related issue in the ioremap() regions
management code that slowed down significantly after CPUs had been
allowed to enter idle states even if they'd had RCU callbakcs
queued and triggered some problems in certain proprietary graphics
driver (and elsewhere). The fix replaces synchronize_rcu() in that
code with synchronize_rcu_expedited() which makes the issue go
away. From Konstantin Khlebnikov.
- ACPI LPSS (Low-Power Subsystem) driver fix to handle power
management of the DMA engine included into the LPSS correctly. The
problem is that the DMA engine doesn't have ACPI PM support of its
own and it simply is turned off when the last LPSS device having
ACPI PM support goes into D3cold. To work around that, the PM
domain used by the ACPI LPSS driver is redesigned so at least one
device with ACPI PM support will be on as long as the DMA engine is
in use. From Andy Shevchenko.
- ACPI backlight driver fix to avoid using it on "Win8-compatible"
systems where it doesn't work and where it was used by default by
mistake (Aaron Lu).
- Assorted minor ACPI core fixes and cleanups from Tomasz Nowicki,
Sudeep Holla, Huang Rui, Hanjun Guo, Fabian Frederick, and Ashwin
Chaugule (mostly related to the upcoming ARM64 support).
- Intel RAPL (Running Average Power Limit) power capping driver fixes
and improvements including new processor IDs (Jacob Pan).
- Generic power domains modification to power up domains after
attaching devices to them to meet the expectations of device
drivers and bus types assuming devices to be accessible at probe
time (Ulf Hansson).
- Preliminary support for controlling device clocks from the generic
power domains core code and modifications of the ARM/shmobile
platform to use that feature (Ulf Hansson).
- Assorted minor fixes and cleanups of the generic power domains core
code (Ulf Hansson, Geert Uytterhoeven).
- Assorted minor fixes and cleanups of the device clocks control code
in the PM core (Geert Uytterhoeven, Grygorii Strashko).
- Consolidation of device power management Kconfig options by making
CONFIG_PM_SLEEP select CONFIG_PM_RUNTIME and removing the latter
which is now redundant (Rafael J Wysocki and Kevin Hilman). That
is the first batch of the changes needed for this purpose.
- Core device runtime power management support code cleanup related
to the execution of callbacks (Andrzej Hajda).
- cpuidle ARM support improvements (Lorenzo Pieralisi).
- cpuidle cleanup related to the CPUIDLE_FLAG_TIME_VALID flag and a
new MAINTAINERS entry for ARM Exynos cpuidle (Daniel Lezcano and
Bartlomiej Zolnierkiewicz).
- New cpufreq driver callback (->ready) to be executed when the
cpufreq core is ready to use a given policy object and cpufreq-dt
driver modification to use that callback for cooling device
registration (Viresh Kumar).
- cpufreq core fixes and cleanups (Viresh Kumar, Vince Hsu, James
Geboski, Tomeu Vizoso).
- Assorted fixes and cleanups in the cpufreq-pcc, intel_pstate,
cpufreq-dt, pxa2xx cpufreq drivers (Lenny Szubowicz, Ethan Zhao,
Stefan Wahren, Petr Cvek).
- OPP (Operating Performance Points) framework modification to allow
OPPs to be removed too and update of a few cpufreq drivers
(cpufreq-dt, exynos5440, imx6q, cpufreq) to remove OPPs (added
during initialization) on driver removal (Viresh Kumar).
- Hibernation core fixes and cleanups (Tina Ruchandani and Markus
Elfring).
- PM Kconfig fix related to CPU power management (Pankaj Dubey).
- cpupower tool fix (Prarit Bhargava)"
* tag 'pm+acpi-3.19-rc1' of git://git.kernel.org/pub/scm/linux/kernel/git/rafael/linux-pm: (120 commits)
i2c-omap / PM: Drop CONFIG_PM_RUNTIME from i2c-omap.c
dmaengine / PM: Replace CONFIG_PM_RUNTIME with CONFIG_PM
tools: cpupower: fix return checks for sysfs_get_idlestate_count()
drivers: sh / PM: Replace CONFIG_PM_RUNTIME with CONFIG_PM
e1000e / igb / PM: Eliminate CONFIG_PM_RUNTIME
MMC / PM: Replace CONFIG_PM_RUNTIME with CONFIG_PM
MFD / PM: Replace CONFIG_PM_RUNTIME with CONFIG_PM
misc / PM: Replace CONFIG_PM_RUNTIME with CONFIG_PM
media / PM: Replace CONFIG_PM_RUNTIME with CONFIG_PM
input / PM: Replace CONFIG_PM_RUNTIME with CONFIG_PM
leds: leds-gpio: Fix multiple instances registration without 'label' property
iio / PM: Replace CONFIG_PM_RUNTIME with CONFIG_PM
hsi / OMAP / PM: Replace CONFIG_PM_RUNTIME with CONFIG_PM
i2c-hid / PM: Replace CONFIG_PM_RUNTIME with CONFIG_PM
drm / exynos / PM: Replace CONFIG_PM_RUNTIME with CONFIG_PM
gpio / PM: Replace CONFIG_PM_RUNTIME with CONFIG_PM
hwrandom / exynos / PM: Use CONFIG_PM in #ifdef
block / PM: Replace CONFIG_PM_RUNTIME with CONFIG_PM
USB / PM: Drop CONFIG_PM_RUNTIME from the USB core
PM: Merge the SET*_RUNTIME_PM_OPS() macros
...
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The SET_PM_RUNTIME_PM_OPS() and SET_RUNTIME_PM_OPS() macros are
identical except that one of them is not empty for CONFIG_PM set,
while the other one is not empty for CONFIG_PM_RUNTIME set,
respectively.
However, after commit b2b49ccbdd54 (PM: Kconfig: Set PM_RUNTIME if
PM_SLEEP is selected) PM_RUNTIME is always set if PM is set, so one
of these macros is now redundant.
For this reason, replace SET_PM_RUNTIME_PM_OPS() with
SET_RUNTIME_PM_OPS() everywhere and redefine the SET_PM_RUNTIME_PM_OPS
symbol as SET_RUNTIME_PM_OPS in case new code is starting to use the
macro being removed here.
Reviewed-by: Ulf Hansson <ulf.hansson@linaro.org>
Acked-by: Kevin Hilman <khilman@linaro.org>
Signed-off-by: Rafael J. Wysocki <rafael.j.wysocki@intel.com>
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If the post request is cancelling the channel and descriptor and which are
equal to host->dma_current and host->dma_desc_current respectively, then it
makes sense to reset these pointers to NULL, so that the driver does not
reference it.
Also the host_cookie can be reset to 0 in cases of error, so that the
core could reissue the same mmc_request.
This patch was tested with 'mmc: core: fix prepared requests while doing
bkops' to fix the below issue.
mmci-pl18x 12400000.sdcc: error during DMA transfer!
Unable to handle kernel paging request at virtual address 40000000
pgd = c0204000
[40000000] *pgd=00000000
Internal error: Oops: 805 [#1] SMP ARM
Modules linked in: ipv6 ath6kl_sdio ath6kl_core
CPU: 0 PID: 0 Comm: swapper/0 Tainted: G W 3.17.0-rc7-linaro-multi-v7 #1
task: c0c9d7e0 ti: c0c92000 task.ti: c0c92000
PC is at v7_dma_inv_range+0x34/0x4c
LR is at __dma_page_dev_to_cpu+0x80/0x100
pc : [<c021efc0>] lr : [<c021af18>] psr: 400f0193
sp : c0c93e20 ip : c0c9a478 fp : c08ea538
r10: c0c9f548 r9 : 00000002 r8 : e97d9000
r7 : 00000200 r6 : c0c9d504 r5 : c0db0880 r4 : 00000000
r3 : 0000003f r2 : 00000040 r1 : 40000200 r0 : 40000000
Flags: nZcv IRQs off FIQs on Mode SVC_32 ISA ARM Segment kernel
Control: 10c5787d Table: a9ef406a DAC: 00000015
Process swapper/0 (pid: 0, stack limit = 0xc0c92250)
Stack: (0xc0c93e20 to 0xc0c94000)
3e20: c021f058 e9a17178 e9a171bc e99dfd6c 00000001 00000001 e995de10 00000002
3e40: 00000000 c021b574 00000000 c04bc4a4 00000000 e9b49ac0 c0ce6e6c e99dfda4
3e60: 00000088 e9810780 c0d8291c c072ea58 00000000 c072d3fc 00000000 c072f534
3e80: 00000000 e9b49ac0 00000100 c0c9a444 00000088 c072f6b4 c072f5d4 e9d40080
3ea0: e98107dc 00000000 00000000 c0280a60 00000000 7d55bf61 e9810780 e98107dc
3ec0: 00000000 f0002000 c0d460e8 c0d460e8 c0c92000 c0280b60 e9810780 c0ce7190
3ee0: 00000000 c028369c c02835f4 00000088 00000088 c0280278 c0c8ec70 c020f080
3f00: f000200c c0c9a958 c0c93f28 c02088e4 c04bd630 c04bd5bc 200f0013 ffffffff
3f20: c0c93f5c c0212800 00000001 a987c000 c0c93f3c c04bd574 00000000 0000015b
3f40: ea7a0e40 00000000 c0d460e8 c0d460e8 c0c92000 c08ea538 29b12000 c0c93f70
3f60: c04bd630 c04bd5bc 200f0013 ffffffff c04bd574 c071bd24 7d50c9b4 c0719a44
3f80: 7d50c9b4 0000015b c0c9a498 c0c92028 c0c9a498 c0c9a4fc ea7a0e40 c0c8ee38
3fa0: c0d460e8 c0276198 00000000 c0d8291a 00000000 c0c9a400 00000000 c0be0bc4
3fc0: ffffffff ffffffff c0be05f8 00000000 00000000 c0c533d8 c0d82ed4 c0c9a47c
3fe0: c0c533d4 c0c9e870 8020406a 511f06f0 00000000 80208074 00000000 00000000
[<c021efc0>] (v7_dma_inv_range) from [<c021af18>] (__dma_page_dev_to_cpu+0x80/0x100)
[<c021af18>] (__dma_page_dev_to_cpu) from [<c021b574>] (arm_dma_unmap_sg+0x5c/0x84)
[<c021b574>] (arm_dma_unmap_sg) from [<c072ea58>] (mmci_dma_unmap.isra.16+0x60/0x74)
[<c072ea58>] (mmci_dma_unmap.isra.16) from [<c072f534>] (mmci_data_irq+0x1fc/0x29c)
[<c072f534>] (mmci_data_irq) from [<c072f6b4>] (mmci_irq+0xe0/0x114)
[<c072f6b4>] (mmci_irq) from [<c0280a60>] (handle_irq_event_percpu+0x78/0x134)
[<c0280a60>] (handle_irq_event_percpu) from [<c0280b60>] (handle_irq_event+0x44/0x64)
[<c0280b60>] (handle_irq_event) from [<c028369c>] (handle_fasteoi_irq+0xa8/0x1a8)
[<c028369c>] (handle_fasteoi_irq) from [<c0280278>] (generic_handle_irq+0x2c/0x3c)
[<c0280278>] (generic_handle_irq) from [<c020f080>] (handle_IRQ+0x40/0x90)
[<c020f080>] (handle_IRQ) from [<c02088e4>] (gic_handle_irq+0x38/0x68)
[<c02088e4>] (gic_handle_irq) from [<c0212800>] (__irq_svc+0x40/0x54)
Exception stack(0xc0c93f28 to 0xc0c93f70)
3f20: 00000001 a987c000 c0c93f3c c04bd574 00000000 0000015b
3f40: ea7a0e40 00000000 c0d460e8 c0d460e8 c0c92000 c08ea538 29b12000 c0c93f70
3f60: c04bd630 c04bd5bc 200f0013 ffffffff
[<c0212800>] (__irq_svc) from [<c04bd5bc>] (msm_cpu_pm_enter_sleep+0x48/0x4c)
[<c04bd5bc>] (msm_cpu_pm_enter_sleep) from [<c071bd24>] (qcom_lpm_enter_spc+0x20/0x2c)
[<c071bd24>] (qcom_lpm_enter_spc) from [<c0719a44>] (cpuidle_enter_state+0x44/0xf0)
[<c0719a44>] (cpuidle_enter_state) from [<c0276198>] (cpu_startup_entry+0x1f4/0x238)
[<c0276198>] (cpu_startup_entry) from [<c0be0bc4>] (start_kernel+0x384/0x390)
Code: 1e070f3e e1110003 e1c11003 1e071f3e (ee070f36)
---[ end trace cf6cb3f6432c9834 ]---
Kernel panic - not syncing: Fatal exception in interrupt
Signed-off-by: Srinivas Kandagatla <srinivas.kandagatla@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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commit 98e90de99a0c43bd434da814c882c4332441871e
"mmc: host: switch OF parser to use gpio descriptors"
switched the semantic behaviour of card detect and read
only flags such that the inversion capability flag would
only be set if inversion was explicitly specified in the
device tree, in the hopes that no-one was using double
inversion.
It turns out that the XOR:ing between the explicit
inversion was indeed in use, so we need to restore the
old semantics where both ways of inversion are checked
and the end result XOR:ed.
Reported-by: Javier Martinez Canillas <javier@dowhile0.org>
Tested-by: Javier Martinez Canillas <javier@dowhile0.org>
Signed-off-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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This patch renames sdio flag in vendor data to st_sdio, as this flag is
only used to enable ST specific sdio setup. This will also ensure that
the ST specfic setup is not done on other vendor like Qualcomm.
Originally the issue was detected while testing WLAN ath6kl on IFC6410
board with APQ8064 SOC.
Signed-off-by: Srinivas Kandagatla <srinivas.kandagatla@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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This patch adds sdio enable mask in variant data, SOCs like ST have
special bits in datactrl register to enable sdio. Unconditionally setting
this bit in this driver breaks other SOCs like Qualcomm which maps this
bits to something else, so making this enable bit to come from variant
data solves the issue.
Originally the issue is detected while testing WLAN ath6kl on Qualcomm
APQ8064.
Reviewed-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Srinivas Kandagatla <srinivas.kandagatla@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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Currently the MMCI driver will only handle GPIO descriptors
implicitly through the device tree probe glue in mmc_of_init(),
but devices instatiated other ways such as through board files
and passing descriptors using the GPIO descriptor table will
not be able to exploit descriptors.
Augment the driver to look for a GPIO descriptor if device
tree is not used for the device, and if that doesn't work,
fall back to platform data GPIO assignment using the old
API. The end goal is to get rid of the platform data integer
GPIO assingments from the kernel.
This enable the MMCI-embedding platforms to be converted to
GPIO descritor tables.
Cc: Alexandre Courbot <gnurou@gmail.com>
Cc: Russell King <linux@arm.linux.org.uk>
Signed-off-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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On Qualcomm APQ8064 SOCs, SD card controller has an additional glue
called DML (Data Mover Local/Lite) to assist dma transfers.
This hardware needs to be setup before any dma transfer is requested.
DML itself is not a DMA engine, its just a gule between the SD card
controller and dma controller.
Most of this code has been ported from qualcomm's 3.4 kernel.
This patch adds the code necessary to intialize the hardware and setup
before doing any dma transfers.
Reviewed-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Srinivas Kandagatla <srinivas.kandagatla@linaro.org>
Reviewed-by: Stephen Boyd <sboyd@codeaurora.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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Commit "mmc: mmci: Handle CMD irq before DATA irq", caused an issue
when using the ARM model of the PL181 and running QEMU.
The bug was reported for the following QEMU version:
$ qemu-system-arm -version
QEMU emulator version 2.0.0 (Debian 2.0.0+dfsg-2ubuntu1.1), Copyright
(c) 2003-2008 Fabrice Bellard
To resolve the problem, let's restore the old behavior were the DATA
irq is handled prior the CMD irq, but only for the arm_variant, which
the problem was reported for.
Reported-by: John Stultz <john.stultz@linaro.org>
Cc: Peter Maydell <peter.maydell@linaro.org>
Cc: Russell King <linux@arm.linux.org.uk>
Tested-by: Kees Cook <keescook@chromium.org>
Tested-by: John Stultz <john.stultz@linaro.org>
Cc: <stable@vger.kernel.org> # v3.15+
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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This patch won't change the behavior of how mmci deals with CMD irqs.
By moving code from mmci_irq() to mmci_cmd_irq(), we getter a better
overview of what going on.
Cc: Peter Maydell <peter.maydell@linaro.org>
Cc: John Stultz <john.stultz@linaro.org>
Cc: Russell King <linux@arm.linux.org.uk>
Tested-by: Kees Cook <keescook@chromium.org>
Tested-by: John Stultz <john.stultz@linaro.org>
Cc: <stable@vger.kernel.org> # v3.15+
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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We don't need to verify the content of the status register twice, while
we are about to handle a DATA irq. Instead let's leave all verification
to be handled by mmci_data_irq().
Cc: Peter Maydell <peter.maydell@linaro.org>
Cc: John Stultz <john.stultz@linaro.org>
Cc: Russell King <linux@arm.linux.org.uk>
Tested-by: Kees Cook <keescook@chromium.org>
Tested-by: John Stultz <john.stultz@linaro.org>
Cc: <stable@vger.kernel.org> # v3.15+
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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This patch adds a fake Qualcomm ID 0x00051180 to the amba_ids, as Qualcomm
SDCC controller is pl180, but amba id registers read 0x0's.
The plan is to remove SDCC driver totally and use mmci as the main SD
controller driver for Qualcomm SOCs.
Signed-off-by: Srinivas Kandagatla <srinivas.kandagatla@linaro.org>
Reviewed-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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MCIFIFOCNT register behaviour on Qcom chips is very different than the other
pl180 integrations. MCIFIFOCNT register contains the number of
words that are still waiting to be transferred through the FIFO. It keeps
decrementing once the host CPU reads the MCIFIFO. With the existing logic and
the MCIFIFOCNT behaviour, mmci_pio_read will loop forever, as the FIFOCNT
register will always return transfer size before reading the FIFO.
Also the data sheet states that "This register is only useful for debug
purposes and should not be used for normal operation since it does not reflect
data which may or may not be in the pipeline".
This patch implements a qcom specific get_rx_fifocnt function which is
implemented based on status register flags. Based on qcom_fifo flag in
variant data structure, the corresponding get_rx_fifocnt function is selected.
Signed-off-by: Srinivas Kandagatla <srinivas.kandagatla@linaro.org>
Reviewed-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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On Controllers like Qcom SD card controller where cclk is mclk and mclk should
be directly controlled by the driver.
This patch adds support to control mclk directly in the driver, and also
adds explicit_mclk_control flag in variant structure giving more flexibility
to the driver.
Signed-off-by: Srinivas Kandagatla <srinivas.kandagatla@linaro.org>
Reviewed-by: Linus Walleij <linus.walleij@linaro.org>
[Ulf Hansson] Fixed checkpatch warning
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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Some of the controller have maximum supported frequency, This patch adds
support in variant data structure to specify such restrictions. This
gives more flexibility in calculating the f_max before passing it to
mmc-core.
Signed-off-by: Srinivas Kandagatla <srinivas.kandagatla@linaro.org>
Reviewed-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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On some SOCs like Qcom there are explicit bits in the command register
to specify if its a data transfer command or not. So this patch adds
support to such bits in variant data, giving more flexibility to the
driver.
Signed-off-by: Srinivas Kandagatla <srinivas.kandagatla@linaro.org>
Reviewed-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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This patch adds edge support for data and command out to variant structure
giving more flexibility to the driver to support more SOCs which have
different clock register layout.
Without this patch other new SOCs like Qcom will have to add more code to
special case them
Signed-off-by: Srinivas Kandagatla <srinivas.kandagatla@linaro.org>
Reviewed-by: Linus Walleij <linus.walleij@linaro.org>
[Ulf Hansson] Resolved conflict
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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This patch adds 8bit bus enable to variant structure giving more flexibility
to the driver to support more SOCs which have different clock register layout.
Without this patch other new SOCs like Qcom will have to add more code
to special case them.
Signed-off-by: Srinivas Kandagatla <srinivas.kandagatla@linaro.org>
Reviewed-by: Linus Walleij <linus.walleij@linaro.org>
[Ulf Hansson] Resolved conflict
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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This patch adds ddrmode mask to variant structure giving more flexibility
to the driver to support more SOCs which have different datactrl register
layout.
Without this patch datactrl register is updated with incorrect ddrmode mask,
resulting in failures on Qualcomm SD Card Controller.
Signed-off-by: Srinivas Kandagatla <srinivas.kandagatla@linaro.org>
Reviewed-by: Linus Walleij <linus.walleij@linaro.org>
[Ulf Hansson] Resolved conflict
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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Instance of this IP on Qualcomm's SOCs has bit different layout for datactrl
register. Bit position datactrl[16:4] hold the true block size instead of power
of 2.
Signed-off-by: Srinivas Kandagatla <srinivas.kandagatla@linaro.org>
Reviewed-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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On Qcom SD Card controller POWER, CLKCTRL, DATACTRL and COMMAND registers
should be updated in MCLK domain, and writes to these registers must be
separated by three MCLK cycles. This resitriction is not applicable for
other registers. Any subsequent writes to these register will be ignored
until 3 MCLK have passed.
One usec delay between two CMD register writes is not sufficient in the
card identification phase where the CCLK is very low. This patch replaces
a static 1 usec delay to use mmci_reg_delay function which can provide
correct delay depending on the cclk frequency.
Without this patch the card is not detected.
Signed-off-by: Srinivas Kandagatla <srinivas.kandagatla@linaro.org>
Reviewed-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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This patch replaces a constant used in calculating timeout with a proper
macro. This is make code more readable.
Signed-off-by: Srinivas Kandagatla <srinivas.kandagatla@linaro.org>
Reviewed-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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git://git.kernel.org/pub/scm/linux/kernel/git/cjb/mmc
Pull MMC update from Chris Ball:
"MMC highlights for 3.16:
Core:
- support HS400 mode of eMMC 5.0, via DT bindings mmc-hs400-1_{2,8}v
- if card init at 3.3v doesn't work, try 1.8v and 1.2v too
Drivers:
- moxart: New driver for MOXA ART SoCs
- rtsx_usb_sdmmc: New driver for Realtek USB card readers
- sdhci: Large rework around IRQ/regulator handling, remove card_tasklet
- sdhci-pci-o2micro: Add SeaBird SeaEagle SD3 support
- sunxi: New driver for Allwinner sunxi SoCs
- usdhi6rol0: New driver for Renesas SD/SDIO controller"
* tag 'mmc-updates-for-3.16-rc1' of git://git.kernel.org/pub/scm/linux/kernel/git/cjb/mmc: (95 commits)
mmc: sdhci-s3c: use mmc_of_parse and remove the card_tasklet
mmc: add a driver for the Renesas usdhi6rol0 SD/SDIO host controller
mmc: sdhci-of-esdhc: Fixup compile error
mmc: tegra: fix reporting of base clock frequency
mmc: tegra: disable UHS modes
mmc: sdhci-dove: use mmc_of_parse() and remove card_tasklet CD handler
MAINTAINERS: mmc: Add path to git tree
mmc: dove: fix missing MACH_DOVE dependency
mmc: sdhci: SD tuning is broken for some controllers
mmc: sdhci-esdhc-imx: fix mmc ddr mode regression issue
mmc: sdhci-pci-o2micro: Add SeaBird SeaEagle SD3 support
mmc: omap_hsmmc: split omap-dma header file
mmc: omap_hsmmc: fix cmd23 multiblock read/write
mmc: omap_hsmmc: use devm_ioremap_resource
mmc: omap_hsmmc: use devm_request_threaded_irq
mmc: omap_hsmmc: use devm_request_irq
mmc: omap_hsmmc: use devm_clk_get
mmc: sunxi: Add driver for SD/MMC hosts found on Allwinner sunxi SoCs
mmc: wmt-sdmmc: Use GFP_KERNEL instead of hard-coded value
mmc: omap: Use DIV_ROUND_UP instead of open coded
...
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Remove the option to provide DMA configuration as platform data,
enforce it through DT.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Cc: Russell King <linux@arm.linux.org.uk>
Cc: Roland Stigge <stigge@antcom.de>
Acked-by: Arnd Bergmann <arnd@arndb.de>
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Remove the option to provide a maximum frequency as platform data,
enforce it through DT.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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Remove the option to provide the flags for mmc capabilities as platform
data, enforce it through DT.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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Remove the option to provide signal direction configuration and
feeback clock as platform data, enforce it through DT.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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This is pure software configuration, which mmci has been supporting for
a while. Let's enable it as default so we can take benefit from it.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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Let mmci DT parser only handle the specific bindings related to mmci
and extend the DT support by converting to the common mmc DT parser.
While both DT and platform data exist, DT takes precedence. If there
are supplied DT data, the card detect and write protect GPIOS are
enforced to be provided through it.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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The ST Micro variant supports the option of using a feedback clock signal in
favor of the clockout pin when latching incoming signals on the data bus.
Since this is matter of how pins are being routed we need to provide a new DT
binding to be able to configure this through DT.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Reviewed-by: Linus Walleij <linus.walleij@linaro.org>
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Some variants have support for indicating the bus signal directions,
which currently are configured through platform data.
Add corresponding DT bindings to enable us to move away from using the
platform data.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Reviewed-by: Linus Walleij <linus.walleij@linaro.org>
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Converting to devm functions to simplify error handling in ->probe() and
to cleanup ->remove().
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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To avoid duplication of code while handling card detect and write
protect GPIO pins/irqs, let's convert to use the mmc gpio API.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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For CONFIG_PM_SLEEP, the device were always left in full power state
after system suspend.
We solely relied on a power domain to put it into low power state,
which is an unreasonable requirement to put on SOCs to implement.
Especially for those SOCs not supporting power domains at all.
Use pm_runtime_force_suspend|resume() as the system suspend callbacks,
to resolve the issue.
Cc: Russell King <linux@arm.linux.org.uk>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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Convert to the SET_PM_RUNTIME_PM macro while defining the runtime PM
callbacks. This means the callbacks becomes available for both
CONFIG_PM_SLEEP and CONFIG_PM_RUNTIME, which is needed to handle the
combinations of these scenarios.
Cc: Russell King <linux@arm.linux.org.uk>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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In runtime suspended state, we are not expecting IRQs and thus we can
safely mask them, not only for pwrreg_nopower variants but for all.
Obviously we then also need to make sure we restore the IRQ mask while
becoming runtime resumed.
Cc: Russell King <linux@arm.linux.org.uk>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
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Added MMC_DDR52 as eMMC's DDR mode distinguished from SD-UHS.
CC: Russell King <linux@arm.linux.org.uk>
Signed-off-by: Seungwon Jeon <tgih.jun@samsung.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Signed-off-by: Chris Ball <chris@printf.net>
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The ux500 variants have HW busy detection support, which is indicated
by the busy_detect flag. For these variants let's enable the
MMC_CAP_WAIT_WHILE_BUSY flag and add the support for it.
The mmc core will provide the RSP_BUSY command flag for those requests
we should care about busy detection. Regarding the max_busy_timeout,
the HW don't support busy detection timeouts so at this initial step
let's make it simple and set it to zero to indicate we are able to
support any timeout.
Cc: Russell King <linux@arm.linux.org.uk>
Cc: Johan Rudholm <jrudholm@gmail.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Signed-off-by: Chris Ball <chris@printf.net>
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